QUOTE=Taylor;32753]I would say that I dont beileve it... In all that days I have hung around with karters I have never seen a little 3hp Briggs and Stratton engine spin that much.
The only motors I have seen spin that much are outlaw karts running methonal and these were 5hp Briggs. With monster billet cams and off-set ground cranks and such.
Unless you have some special goodies and a HUGE cam and a billet rod and billet flywheel there is NO, and I mean NO way a stock briggs with a cam can spin that much without breaking.
Unless I see some video or pictures or something of prove I say its a bunch of BS![/QUOTE]
I can assure you that what I stated was fact. How do I prove it? Can't really.
But I'll give you some back ground on the set up that produced this. First off I use this tachometer. It is a mechanical tachometer accurate to 1% full scale and good for 12,000 RPM:
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The motor was modified top to bottom:
Cylinder head milled .093"
Hand made dead soft .032" copper head gasket.
Stock aluminum bore with multi-piece Briggs chrome rings (zero gap)
Painted piston crown
connecting rod polished 100% with round journals
"Supertanium" socket head cap screws installed in rod.
Dipper cut down
Lightened piston with custom made hollow wrist pin.
Knife edge counter weights on crank
Maximum port on both intake and exhaust:
Visualized with laminar water flow to maximize inlet swirl
indexed "power tip" spark plug
Back cut valves with narrow seats
Reduced tension intake spring to induce valve float and maximize "open time"
Shimmed exhaust valve spring.
Easy-Spin bump on cam removed and base circle polished
home made bronze valve guides with .001 stem clearance
Carb "helix" removed
Air cleaner mount cut out of carb
flywheel od turned to .0005" run out
magneto "shoe" set to absolute minimum clearance
Points sets to .010" to maximize timing.
Throttle stop modified to yield 90 degree maximum opening
And last but not least:
Home made counter weight to replace rod and piston assembly
during balancing by local industrial shop.
This 9,200 RPM was obtained with the bolted down to the work bench with no load. Two of the biggest problems were oil pumping and spark. I was only able to obtain these RPM with a .010 gap. The oil pumping issue was solved with a partial crank case fill.
Granted the RPM was basically a flash reading. It not like it was held there. But it was good for maybe 3 seconds. Just enough time to kick all the oil right out the spring pocket.
Now these are facts. You can call Bull if you like. Rhovis couldn't give a pinch less because he knows what the facts are.